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Plunger Lift Systems
About
Challenges
The well was no longer producing enough oil or gas to run a rod lift system economically during the downturn
Low production, high operating expenses, and high intervention costs caused the well to be shut in the majority of the year
The well was only averaging 5 bbls/d of oil and 68 mcf/d in a 12 month period
Results
Saved the well from P & A, deferring $200,000-$400,000 in P & A costs
Brought the well up to an average of 52 bbls/day and 345 mcf/day, an 842% increase in oil and 451% improvement in gas production in the first month and continued to consistently produce above expectations
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Operator deferred $200,000 - $400,00 in P&A costs and turned a profit by turning their rod lift well into a plunger lift well.
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