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Vortex Jetted Pad

About

Challenges

  • Production from wells needed to be optimized installation of artificial lift

  • Production, downhole velocities, pressures, & tubing performance curves needed to be analyzed

  • Tool selection & operational parameter recommendations were needed

Results

  • 71% uplift in gas production and 157% increase in fluid production

  • Essentially eliminated the operators need to unload wells to tanks & release GHG to atmosphere

  • More consistent and predictable production declines. Effective artificial lift results in stable, steady, & predictable production

  • The operator developed their own best practices, which carried forward, they applied to additional wells

Have a similar problem?

Operator found a 71% uplift in gas production and 157% increase in fluid production after installation of the Xcel Jetted Pad.

For more information about how Well Master can meet your needs, contact us today!

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